Friday, 16 January 2015

E60 530d MOT Fail - Brakes, Trailing Arm

After the horror of the swirl-flap failure and engine swap, the E60 went off the road again at the start of December after an annoying MOT fail on imbalanced brakes, likely discs and pads, and split trailing arm bushes on the N/S. The tester also failed it on a bend in the rim of the N/S/R alloy wheel, which is reasonably bad, but enough to be an MOT fail I am not too sure.

This is the bush on the offending arm with the most play, but I still can't see a major split as I have with other bushes.
Closer inspection reveals what could be a split on the right side of the pic, but it's still not a shut case. Maybe the rubber has separated from the metal outer and is moving around?
Ok, so it's no small dent. The inner rim is bent, where the tyre sits, but I've had similar sized ones before that have been no problem. 
Is it repairable? Perhaps, but I have no spare wheel to use and a replacement is £200. Maybe the MOT tester was having a bad day?

Saturday, 10 January 2015

Update New Year 2015

Not a great deal has been going on in Beemer Lab since the mighty engine swap and not just because I needed a rest.. The E60 went off the road again with an annoying MOT fail at the start of December and thanks to a busy Xmas I'm still in the Compact, so here's some nice Wirral Beemers over the festive season.

West Wal' Compact Club. Be there, or have a proper derrière.
It's my old E21. Wait, no it isn't. Who'd have thought it... another '83 316 in Henna Red, parked just around the corner from my house in Wallasey, as if to taunt me for selling mine. It' on the original 13s and absolutely mint.

Speaking of my old E21, here is a recent picture taken from eBay. Yes, it went up for sale in late November and sold within a week. Jake's asking price was £2250. It is now owned by a lad called Daniel.

Henna Red 635 CSi Highline out in Wallasey / Bidston.
Nicely stanced and rolled E36 Cab on BBS parked up in Moreton.
My Titansilver fleet of 2014. The E46 is gone and the Compact will sadly have to follow when the 5-Series is MOT'd.


Friday, 24 October 2014

E60: Split Vac-line, some boost, weird noises.

The turbo whine and lack of boost has persisted, so I took off the inlet-manifold again to check the vacuum-lines and found one has snapped off. Luckily, there was plenty of hose left to cut it down and push it back onto the T-piece. I re-checked every line twice against the diagrams on RealOEM.com and refitted the manifold, making sure the seals were super flush. Now when I fired up the turbo started making a ridiculous whoosh and dump-valve style hiss, as in the vid below. Some boost had returned too, though not as much as there should be and certainly nothing like the turbo sounded. Still, the vac-line repair did get a result, so it looks there could be life in the turbo yet.


There was nothing else I could do other than pore over the vac-line configuration, so I made this quick one-piece diagram to show the route of the four coming off the servo-pipe to save switching between several diagrams on RealOEM. I then started pulling vac-lines off in order to find the faulty area and, amazingly, managed to get rid of the whoosh/hiss and still have some boost. The turbo is still whistling though and there is not enough pull as you get over 2k rpm, so something is still amiss.

  • Split vac-line to swirl-flaps - Low boost, quiet turbo-whistle higher up.
  • Repaired vac-line - Some boost low down, cuts out higher up. Loud whoosh and hiss noise, turbo-whistle constantly.
  • Vac-hose removed from wastegate - Low boost, quiet turbo-whistle higher up.
  • Swirl-flaps and engine-mount vac-lines switched round - Some boost, no whoosh/hiss, constant turbo whistle, less engine vibration.
The diagrams do not make clear the route of the red/black striped hose on the right of mine. This turned out to be the N/S engine-mount and another scan of RealOEM.com revealed how they work in the pic below. I had wondered about a problem with the engine-mounts anyway, as there seems to be a lot more engine vibration than before, especially on tickover, so my next job will be to find the pipes that link the mounts together and check their condition. They all run through the subframe next to the steering-rack. M57N is a complicated vacuum arrangement.

Wednesday, 15 October 2014

E60: Opening Stuck Bonnet.

PROBLEM:
The annoying turbo whine from my previous post can only be heard while underway and not while stationary, so the bonnet is up and down for every bit of work and test drive. After several such runs, the O/S (driver's side) bonnet latch refused to open. Nearly an hour was spent with a helper pulling the bonnet-lever while I tried to push / pull / wiggle the O/S bonnet up, but it was stuck solid. The front bonnet lip on the E60 (and all modern BMWs) extends right down over the slam-panel / grille and the latches are a good 6 inches up inside it. It's impossible to slide something up through the gap between the rubber seal and pop the latch from outside, as you can with older cars, so I turned to the internet and eventually found a superb solution.

CAUSE:
Yes, this is quite a common problem with the E60, especially when you are working on it at home. The cable splits in two and a separate one runs to each latch. The end of the cable fits through an eyelet on the 'release-switch' and is kept under tension by a plastic collar that fits into a notch in the latch-frame. If the plastic collar pops out of the notch, cable tension is lost and the bonnet-lever simply will not pull the release-switch far enough. Removing the bonnet-lever reveals a plastic-cage with the cable housed deep inside, so yanking that further with a pair of grips won't do either. If you've been working on the front-end of the car and changed the location of the bonnet-latches / slam-panel, even slightly, then there's a high chance the collar will start popping out.

SOLUTION:
There are a few forum threads saying the latch can easily be opened from underneath the car, with the front under-tray removed. This is true, but the E60 engine-bay is so tightly packed there is a bit more to it than that. I have to give props to Kilty1 on forum.BMW5.co.uk, for his amazing guide, linked below:

http://forum.bmw5.co.uk/topic/87159-bonnet-release-not-working/

Getting to the latch requires removal on the front under-tray, both pieces of the O/S brake air-duct and the plastic inlet-pipe that runs to the air-filter. These can all be removed from underneath the car, as shown in Kilty1's guide. He used ramps, though I managed to open mine with the car raised a few inches on an axle-stand. Looking up with a torch, you will just see the latch next to the inner corner of the headlight.

Luckily, my brake duct, inlet pipe and tray were already off as I was working on the car, so I could get straight to the latch and will just show a couple of steps and pics from Kilty1's guide:

1. Reach up and slide a steel-rule or similar slim/flat object into the bottom of the latch, just to the inside of the right-hand spring-wheel [shown on the left in the pic, looking from front]. When the steel-rule is far enough in there should be a small clunk. Now slide the steel-rule quickly out and the bonnet latch should release on the O/S. 
2. The collar doesn't take much to pop out, so to stop it from happening again as soon as you shut the bonnet, wrap a cable-tie round the back of the collar and round through the gap in the steel-frame. It will be solid.

Tuesday, 14 October 2014

E60: Turbo whine and no boost!

With the engine-swap teething problems put to rest and the car back on the road [at last!], there was bound to be a few running faults. All in all its going like a dream, though I would say the engine is a lot noisier and vibrates more than before. This could mainly be due to the lack of acoustic-covers and under-trays as I iron out defects, but not entirely so I will have to look at the pneumatic engine-mounts when I have time.

When I got the car out for a good run, the main problem I notice is a serious lack of boost. The turbo is also making a low-pitch whining noise, which sounds a bit like a police siren. I read that this is the noise of a dying turbo, though I find this a little hard to swallow as it was fine before and I see no reason how being removed from the car for 3 weeks would affect it. Far more likely that I've messed up attaching some vac-line or wire-connector, or lets hope so anyway. It's an annoying whistle, as it can only be heard while driving under load and not when revving at a stop.
  • Turbo can be seen spinning.
  • No front-rear play on spindle-shaft, hardly any left-right play.
  • Pipes from turbo to intercooler and intercooler to inlet OK.
  • Removed and cleaned air-temp. sensor.
  • Some boost air is coming from the intercooler outlet.
Before I diagnose a dead turbo and start spending any more money, I will check the vacuum lines meticulously and also re-check the pipes for splits. The turbo also needs looking at, from the oil-feed to how it's fitting the manifold. The waste-gate doesn't seem to be operating and that seems a bit too serious to be caused by such a small vac-line fault. Ho hum, the saga continues...

Monday, 13 October 2014

E60: PAS-Pump + Exhaust Vibration-Damper.

With everything else apparently working, the 530d was still of the road due to the niggling problem of an un-bleedable PAS-system and rattling exhaust.
  • Bleed PAS-system with cap off reservoir and engine off, by turning the wheel lock to lock about 30 times and adding fluid until no more bubbles were coming out.
  • Remove front-bumper and drive back onto ramps.
  • Locate exhaust onto connecting-rods of vibration-damper.
  • Modify connecting-rods to fit new exhaust position.
  • Refit exhaust and reinforcement-plate.
  • Refit engine centre-undertray.
  • Drive off ramps, refit bumper and test drive!
PAS-Pump Bleed:
This is the hardest to bleed PAS-system I have ever come across, though the pipes / pump have been off the car for 3 weeks and could have allowed the system to drain and fill with air more than before. The pump was whining on tickover and making an almighty groan when turned in either direction. The fluid in the reservoir was also frothy white. To fully bleed it required the engine and reservoir cap to be off and the wheel turned full lock left to right about 30 times. To do this I raised the front of the car on axle-stands so the wheels were still touching, but with hardly any weight on them. The first turns lock to lock gulped the remaining fluid right into the system and so much air was coming out I kept re-checking the pipes for a leak. Eventually, the reservoir had swallowed the last of my bottle of fluid and is just about sitting up to the minimum mark, but still bubbles were popping up as the wheel was turned. The lock to lock business continued with me and my dad taking turns for quite some time until there were finally hardly any tiny bubbles rising to the surface. This whole thing was a job in itself, but the pump is very quiet now and the steering assistance is back.

Exhaust Vibration-Damper:
During the first tests there was an almighty rattle from the exhaust from tickover up to about 2k rpm. I assumed this to be because I had left off the exhaust 'vibration-dampers' that brace the bottom of the cat to the gearbox and stop it shaking. I discarded replacing it at first as, if you don't remember exactly the way it all fits together and start bolting your gearbox and exhaust back on willy nilly, then it's impossible to figure out. The long bracket with 3 holes fits around the edge of the gearbox bell-housing, held in by one of the large E14 and two of the smaller E10 Torx-bolts that hold the box to the engine. The connecting-rods then run from the foremost stud on the cat to the N/S stud on the bracket; and from the rearmost stud on the cat to the O/S stud on the bracket, as shown in the picture from TIS. Only trouble was, neither of the rods went anywhere near the brackets. I'm not sure if the entire engine and gearbox is in a slightly different position from before, or it's just the exhaust out of line, or both, but the eyelets on the left-right rod were about 5mm too long for the studs; and the front-rear ones were almost an inch too short. After 2 frustrating hours spent removing mounts and trying to relocate the gearbox / bracket to meet the exhaust I gave up and decided to modify the connecting-rods to fit the new gap lengths. The only remaining way to adjust exhaust position would be to loosen the two nuts holding the cat to the back of the turbo, only to do this requires the rocker-cover / injectors to come back off and I'm not doing that, for now at least.
The modified connecting-rods are below and, due to lack of time, are rather crudely done. I bent the left-right rod down about 3/4" at a steep angle to take 5mm length out of it and help bring it down to the bracket at a flush angle and works rather well. The front-rear was a bit less neatly done and makes use of a piece of 1mm sheet-steel, cut roughly to an inch square and bolted to the rod. It's not the best workaround in the world, but it gets the job done.
After all that, the 'vibration-damper' did not get rid of the rattle! Instead, I traced the annoying noise to the front rubber-mount a bit further down the pipe. The exhaust was banging right into the side of the metal bracket on the gearbox-mount and a bit of fiddling with the adjustable eyelet managed to separate them and killed the rattle dead, so there you go.


Saturday, 11 October 2014

E60: New Engine finally running!

Changed the injector seals last Sunday and gave the ports another good clean. The mist has stopped, but it still did not want to fire. There is fuel to the injectors and the timing is spot on, so this could only mean 2 things - something electronic isn't working properly, or the entire DDE module has fallen out of sync with the engine...

I don't even want to know what the latter option entails, so carried on swapping sensors on the new engine for those that worked on my old one. I found the crank-sensor was completely covered in dirty oil, in fact the whole slot was filled with it. Engine sensors are funny things and I can see how the oil could stop it from seeing the notch on the flywheel, but it doesn't explain why the engine would not turn over well using a can of Easy-Start. Either way, with the crank-sensor from my original lump in place it fired up straight away! Result.

[Video is with EGR-pipe disconnected and no air-filter / muffler fitted.]


  • PAS-pump sounds like it's dying - extreme whine / groan when the wheel is turned - and is now the only thing keeping her off the road. Will try bleeding tomorrow and maybe fresh fluid, but failing that the pump could have packed in or, worse, I've damaged some of the piping / rack while lifting the engine in.
  • Rear rubber exhaust-hanger missing. TIS says to remove the screws holding the hanger-bracket, not remove the rubber. I cut mine off to hastily get the exhaust down and will have to buy and annoyingly fit a new one.
  • Front exhaust vibration-damper simply will not fit. When fitted to the exhaust, the eyelets on the two connecting-rods are way off the studs on the gearbox-bracket. The left-right rod is only about 5mm out, but the front-rear rod is miles off. I will have to remove the rear and centre brackets and try to relocate the exhaust a bit.
Other than that, no iDrive messages, no engine-management light, no 'Increased Emissions', no leaks, no mist and no funny noises. The gearbox and clutch are working fine and the car is desperate to be driven. Curse that power-steering fault!